A few weeks? More like 180 weeks!
Okay, so I've been a bit busy doing other stuff that tends to bring in some cash. Still, just occasionally I gazed at the box and wondered if it was worth spending a few hours on it.
I had planned on spending the month of April on the rebuilt Scot, but having had a falling out with it last week I was at a bit of a loose end until May arrives. So, I decided it might be fun to have a stab at creating a new roof for 41222. You may recall for various reasons the kit etched roof wasn't quite large enough to fit nicely. Having now got a super snazzy riveting tool, and suitable materials, what was to stop me.
Well, quite a lot, as it turned out.
If you scan back through this thread you will find a section where I had to refit a cylinder wrapper that had become detached. Taking the loco from the box revealed the other side wrapper had decided to do the same trick, so I spent a while repairing that and making good. While I was at it, one of the front vac pipes was loose, so I attempted to repair that. I could not get it to stay firm, so I thought I'd just pour some glue in it later on. As it happened, it fell off during some other repair work, so it's now been reattached firmly. Swings and roundabouts, as they say. While poking about with the cylinders, I decided the draincock operating rods which Best Beloved had concocted from scrap etch, wire and brass screws was a little flimsy. Actually, only the rods were flimsy, so they've been ungummed and will be replaced by something more manly in due course.
Because the model is a mix of metal and plastic - some ingenious repurposing was done to make various components, I have to say - making hot repairs is a bit dicey at times. I think I've made a fairly good bodge of the wrapper repair, and haven't seriously bent any of the wiggly bits yet. Some cleaning up and it'll look okay.
I had made a start on installing washout plugs. I mean I had drilled out holes in the firebox and boiler. I'd bought some new LMS washout plug castings from Laurie Griffin, but when I studied photos they looked a bit chunky. Happily, I'd found a selection of ancient brass cast plugs of smaller diameter in the Bits Box. Although a bit iffy in the casting department, they pass muster.
By this stage I had decided to treat this build as a completion to more or less the standard that Best Beloved had started. If I can improve something I will, but otherwise I will roll with what I can do to finish the loco to an acceptable standard allowing for its various faults and idiosyncrasies.
Of course, the plugs needed to be set into the boiler, as they are a little behind the cladding on the real McCoy. I scratched the brain cell for a bit, and decided that most of the holes were through double thickness brass. If I countersunk the holes to allow the castings to drop in a little further, they'd not look too bad. There was no way they could be installed from within, at any rate. Again, not super high fidelity, but I think they'll do.
As I'd had the boiler assembly on and off a few times, inevitably bits began to work loose. They needed repairing. Two steps forward, one back…
The mixed and matched materials worried me, so I decided it might be safer to carefully remove whitemetal fittings like the front lubricators, which needed their pipework reinstating in any case, so some hot stick work could be done to fit the LG motor fitting apparatus.
To aid fitting the parts, I thought a more permanent fixing of the boiler to the body would be sensible. Someone had drilled and tapped a hole through the cab front sheet into the top of the firebox former, so I wheedled a suitable bolt in and carefully tightened it up. The slight gap at the back of the firebox magically disappeared, but a scale foot space appeared between the smokebox and the saddle. Something was out of alignment, and so far I haven't fathomed just what it might actually be. I suspect the cab is on the squiff, but that wouldn't be the only thing. Anyway, for now I have decided to leave the boiler loose fitted. On with the details. The main parts had been assembled by me all those years ago, so it was a case of fettling and fiddling to actually attached them. Again, it's not perfect, but that is just one of those things due to the varying natures of the component parts used on this loco. Happy that the motor gear sat about right, and having reinstalled the pipe that crosses under the smokebox, I refitted the refurbished lubricators.
Having sat back and reviewed things, while it had been a frustrating day of stops and starts, it's actually not too bad in the end. The tank tops need detailing, the cab needs more fitting out, there are some chassis details to find and fit, and the rear of the bunker needs the ladder putting back, but aside from all that and the roof, I can think about getting it painted.
Possibly.