This morning I laid the "portable" track, and collected two wagon loads of ballast to finally level off and finish the last panel of the curve. I then took the opportunity to clear the worksite of another six rubble sacks full of topsoil, by transporting them in the opposite direction.
I had said yesterday that I would apply some graphite to the wheels of one wagon to test the difference (if any) in performance. Unfortunately, I could not find my old faithful, big, thick graphite stick anywhere! I just had to put up with the awful, familiar grinding and binding until the job was done!
I was still collapsed in my armchair and having a break from all my exertions in the heat of the sun, when Glenn turned up. As we discussed the dragging wagon issues, he said his wife (also an artist) had got some pencil shaped graphite sticks. A quick call home, and a tin was offered for the experiment, so I suggested that if he brought the children round after school, we could carry out a proper trial!
In retrospect, it was a Friday afternoon, and the little ones were just a bit too "hyped" to be anything other than a handful. Glenn seemed to be perfectly happy with being left in sole charge of the locomotive - while mayhem was carrying on everywhere else in the garden!
The eased curve, it has to be said, is an improvement over the previous alignment, but the loco still slowed to a crawl - even running light engine on full regulator - when hauling an adult on the tender though! Sadly, the tendency of the engine to climb the rail when pushing stock in reverse was still happening.
Then the graphite was applied, first to the treads and flanges of the tender... to be followed later by one of the wagons...
Wheeeeeeeeeeeeeeeeeee!
Away they went! What a jaw dropping transformation!

I didn't get to have a go myself... but then I might have had some difficulty catching up with them?!
Having to stand and carefully observe the behaviour of the stock, I noticed that even though the friction on all wheels had been so drastically reduced, the engine was still nonetheless trying to "kick-out" on the rear drivers when pushing.
After a while, it became apparent that the leading driving wheel springs are simply far too "soft"! I am fairly confident that exchanging them with something a bit stiffer will do the trick.
I do still want to attend to those awkwardly profiled flanges, although the degree of urgency has subsided somewhat. The contact between the flange and inner face of the rail head, however slight that may be, remains an obvious issue, but clearly this experiment has conclusively revealed that the major factor is indeed the extreme angles at the fulcrum points on the longer wheelbase vehicles. I do wonder if this particular problem might be exacerbated by the use of nylon wheels, where a degree of flexibility in the material creates a significantly larger "footprint" than any steel tyred equivalent?
The next bit of fun will be trying to work out an efficient method for "topping up" those treads. I certainly won't want to be upending the wagons and doing a load of "scribbling" on a remotely regular basis, that's for sure!
Pete.