Just a bit of an update after today's work...
The cab consoles, bulk heads and cab interiors of 40126 sprayed and ready for detailing:
The underframe, bogie side frames and boiler water tank just about complete on 40060. They only need a few details added like water/ fuel gauges and all supplementary pipework/ vents/ fillers painting:
Having spent a little time trying to achieve the split axles for these locos I decided that I needed an alternative method to providing some spring loading to each bogie middle main wheel axles. Up to press I have used the method that Cliff Williams used on one of his class 40 builds. This employed a U shaped piece of 0.7mm wire which had a piece of brass soldered to it thereby allowing the unit to be fixed to the bogie frame by a nut and counter sunk machine screw. The arms of the U then fit inside some brass tube soldered to the top hats, thus providing the spring load for the centre axle. This does work very well but as you can imagine there is now a common link between the two top hats which would render the split axle method useless.
So I had a bit of a trial (and lots of errors) before I came up with a very simple solution. Like Cliffs method I wanted the springs to be removable for maintenance purposes. Here's what I came up with:
Yes, it does look rather simple and I have no idea why it took me so long to arrive at the solution to be honest. But as you can see the springs (lengths of 0.7mm wire) are like extended split pins (the pic above is the prot-type and the final ones are much neater!!). This allows their removal but also stops any movement. As the springs are independent they need a little bit of tweaking to get the correct applied force to both top hats but once set they work very well. They are held onto the bogie frames by small U shaped wires that are pushed into drilled holes then glued.
I have also persevered with making the split axles and since I did not have access to a pillar drill today decided that I would try to drill the starting holes with a small electric hand drill. This worked remarkably well and with a 0.8mm drill bit too! The only down side is I had to be rather careful as I had nothing to hold the axles as I drilled except my fingers. Thankfully all 8 plus two thumbs remain intact
I found this method much easier than using the pillar drill as I could feel how much work the drill bit was doing..... as a result I did not break any bits, yet with the pillar drill I broke a lot!!!
So out with the Devcon 2 ton tomorrow and hopefully I'll have enough split axles for two bogies
Cheers
Lee